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Summary

Date of Test4/8/2018
ParticipantsSteve Bauchanan, Mark Dunk,  Stephen Cholvat, Jack Paduchowski
Minutes Flown (hex)

~20minutes

Minutes Flown (quad)


Objectives

  •  Basic tuning w/ 15" prop
  •  RTL/Autonomous Flight
  •  Loiter
  •  Test thrust with 1 battery instead of 2

Problems Encountered

  • Compass drift caused loiter to drift and go in circles
  • Forgot to charge the taranis
  • Yaw P term was too low, causing yaw overshoot
  • Correctly did RTL
  • Hovering was at ~55%

Tasks Before Next Test

  • Invesigate increased baud rate
  • Mount FPV gear and egg grabber
  • Compass drift
  • cache maps
  • charge computers
  • Investigate higher kV motors

Videos (optional)

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