Attendance
Agenda
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General updates
LTE had no issues!
Phone fixed it - that is the only thing that changes
Didn’t fly for long
drone had bad yaw control. realigned yaw midair a lot. jerky yaw motion during flight.
EKF failures(?)
landed in transitional motion and broke a T mount landing gear.
Compass variations?
recalibrating compass
maybe with phone too close? - if recalibration doesn’t work try that
main xt90 started popping (nearby)
from ESC and not XT90.
capacitor charging? → worth looking into wiring
Two people not enough for a 2 drone flight test. need more people monitoring GS (+visual observers..)
Propulsion + Control
Action items / blockers:
Updates:
< Decision documentation >
Mech | ||
Electrical | ||
LED board | Daniel & Parker reviewing LED board rev 1.1 It’s replaceable with other things (COTS) if necessary Can bypass issues on the 1.0 version if need be - Nathan Green Follow up after meeting for who’s working on LED board. if not done by end of week need to start looking at COTS options | |
EFS | LED board | Owen Grimm Made it blinkingtou touch up connections with solder if one LED is not working consistently
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Sensing
Action items / blockers:
Updates:
< Decision Documentation >
Mech | ||
Electrical | Rangefinder Harness |
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EFS | OFS? |
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Autonomy |
Video System
Action items / blockers:
Updates:
Mech |
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Electrical | VTX Wiring |
OSD did have issues still but it probably was due to channel conflict with the arm switch. |
EFS | ||
Autonomy | LTE Communication | Writing module to convert to JPEG now Phone replacing the LTE hat? → Nathan Green
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Command + Telem
Action items / blockers:
Updates:
Mech | Gemini case | Up for review, review was sent this morning! will be printed following revision https://discord.com/channels/776618956638388305/1221565078135115826 Please read the design document in this thread! (if you are interested in the case) |
Electrical | ELRS Gemini PCB | XT30 Connector pinout on the pcb is wrong (5V and Gnd pin are swapped), but still fixable with harness e.g. with XT60 connector: we need a harness that runs XT60M +ve ---------- XT30F -ve XT60M -ve ------------ XT30F +ve |
EFS | ELRS for comp |
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Autonomy | Pathing | Changed the last command to be a land command. Should integrate pathing and auto landing script together.
CONOPS specifies we need to be within 5 meter radius of each waypoint… Anthony Luo - splining would keep the drone where you want it |
Airframe - General
Action items / blockers:
Waterproofing, new cabin, seats, cargo area
Updates:
< Decision Documentation >
Mech | Pegasus 2.0 |
Before exams, peggy 2 should exist/ nearly exist. → beginning of next term is just testing! (will be handed off to EE to wire) summer term starts May 6. We have 2-3 weeks of testing. Peggy 1 cabin internals?
Peggy 2 cabin internals prioritized
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Electrical | ||
EFS | ||
Autonomy |
Tracking Antenna - General
Action items / blockers:
Updates:
< Decision Documentation >
Mech | Improvements |
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Electrical | custom PCB | review in progress |
Arduino antenna | PCB ordered | |
EFS | Arduino Tracking Antenna | A lot of stuff are broken due to a circuit short
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Autonomy |
General Updates
Yuchen working on getting stick time !