2024-05-18 Pegasus Pre-Competition Test
Admin Preparation
Requested By | @Nathan Green @Yuchen Lin @Daniel Puratich |
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Goal Summary | Final test before competition. |
Status? | DRAFT / SUBMITTED / WAITING FOR SUB-TEAM REVIEW / APPROVED |
Desired Airframe | Pegasus 1 |
Date(s) | 18th May 2024 |
Testplan
Necessary Preparation
Explain what capacity you need, what needs to be mounted, etc.
Necessary items:
Jetson
CV camera
< rfd900 >
etc
Flight characteristics needed:
Flight speed
flight distance
max altitude
< etc >
Comms / Support needed:
Autonomous/repeatable missions
ability to hold location within +/- X meters
FPV Video from the drone?
etc….
Mandatory Attendees
This is a section for all attendees from your subteam which will be present for this flight test. (because they are testing their products, or otherwise)
Name | Phone # | Sub-team | Role |
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Smile Khatri | 8076320853 | Mech |
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Flightline Team
Name | Phone # | Role | Reason |
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@Nathan Green |
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@Yuchen Lin |
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@Daniel Puratich |
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@Amy Hu |
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@Smile Khatri |
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@Tong Zhang |
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@Emma Chan |
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@Hardy Yu |
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Pre-Flight Checklists
Flight Test Timeline
note test 1 is competition task 1 and test 2 is competition task 2
Date/Time | Action | Notes |
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lunch time ish | Briefing @ WARG Bay |
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| Arrival at Flight Test Location |
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| Experiment with tracking antenna |
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| Bring equipment to flightline |
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| Test1 card 1 | @Hardy Yu manually track the drone RTL because RC failsafe |
| Configure direct binding phrase to use normal controller elrs instead of gemini |
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| Test 1 card 1 | @Nathan Green |
| Test 2 card 1 practice #1 | @Nathan Green |
| Test 2 card 1 practice #2 | @Nathan Green |
| switch battery |
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| Test 2 card 1 practice #3 | @Nathan Green |
| Test 2 card 1 practice #4 | @Nathan Green |
| Test 2 card 1 practice #5 | @Yuchen Lin |
| Presentation Photos |
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Start 4:30pm | Debrief |
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DEBRIEF
Flight test debrief report
Before Card 1:
Before departure
@Yuchen Lin didn’t logistic going to flight test → next time book the car beforehand + long weekend machine shop does not open
@Yuchen Lin @Hardy Yu Testing with huston → connected to mission planner and able to forward the message(test 2 times)
first one does not flash the latest code
second one see tracking antenna working as expected
After departure
pre-flight tracking antenna testing: (no code change)
Keep rotating without stop and does not work
After adjust to the north keep rotating clockwise
does not help after adding delay
Card 1 Test 1
Flight planning
conduct half task 1 goal (1.5 lap)
Card 1 Test 1 retry 1
Card 2 Test 1
Outcomes
confident in flight characteristics of the drone and electrical robsutness
spline waypoints looked good during flight but looks poor on mission plannre
low confidence in custom rf links and tracking antenna
not using tracking antenna for comp → cc @Daniel Puratich to bringup at AEAC
Gemini board was low link quality
try another gemini board and see if it works
@Nathan Green apply new mag fit data based on today’s data
Check weather before comp.
Flightline tasks:
bring vtx tower, drone(path uploaded, battery in , shourds on), controller and the monitor
Before takeoff
@Daniel Puratich conduct the pre takeoff checklist
manually toggle safety switch
confirm take off flight mode
arm in auto