- Created by Daniel Puratich, last modified by Mena Azab on 2023-11-22
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Introduction
Please add your name here if you are present during the meeting! Feel free to add it in advance if you plan on attending.
Tuned Three Axies successfully on Houston!
New camera mount pog
Flew drone manually
Collected images on first flight
RPi did not work after that
suspecting temperature?
if temp was around zero,
Low voltage on power
possible issue on buck converter or temperature
looking at RPi readout
should temperature test buck board
possibly wiring voltage drop is the issue as well?
Should check temperature operating range of all autonomy components as we get into winter
AEAC Townhall #1
Daniel Puratich Attended
Talk about date and time
see the meeting notes:
Systems
Frame is currently disassembled following the flight test
arms removed currently
nothing was noted wearing early
should inspect holes? Conall Kingshott will look tmrw, but should be goooooood
wear that happened to wires is most likely from monster mount install so not going to focus on correction to the rest of arm stuff
awaiting heatshrink for wires to reassemble
We considered options for removing thread-to-wire contact in the system
Conall Kingshott thinks this isn’t necessary. Do others disagree?
Bolts that aren’t threaded on the top in such a way that would address this are not easily available
Lots of effort, likely wasnt the problem
No big updates from last week!
Composites Canada resin and hardener is here (hopefully, needs to be inspected)
will be doing layups for cabin on Sunday
Orderred skeleton tubes from Aliexpress
hopefully arrive soon!
Shrouds are made and cut
done on bandsaw instead of waterjet bc pre thin
layups that were done last week are good
Gotta look at connecting them to clips.
Will use some sort of adhesive.
Going to consider covering bolt threads.
Possibly heat shrink?
Flight test to test these!
see below!
360 Lidar flight test with Houston!
Should consider a mount to get this on Houston?
Lidar is very expensive so should have a thought out about mount for this!
Anthony Luo to list constraints in a conf document!
Preferably as a subpage to Sensors
This will help mech understand const
From last weeks EE meeting:
Majority of technical details related to choosing voltage divider values into ADC figured out after taking into account the equivalent circuit in the ADC that contributes to the input impedance.
Finishing up LTspice simulation to try to validate proper equivalent input impedance after taking into account the shottky diode and low pass filter.
Still trying to figure out pros and cons in deciding to put RPP across the input voltage from the batteries or just the input into the 5V and 12V buck regulators.
(No Updates)
Anthony Zhelnakov Mena Azab will meet with Daniel to go over this.
Bullet connectors soldered and frayed wire repaired.
Will need to order more 16awg wire unless we know where the remaining wire we ordered in the summer went.
Goal to have prototype on perfboard ready for end of term.
Working on schematic design and LED selection.
Working on pin conflict to support SD card for logging
Ayoung Eun Aryan Kashem is currently working on Arduino version of the tracking antenna
Idea: mostly off the shelf, quick iteration, and can test the tracking antenna algorithm
Using Arduino Mega that’s sitting in our bay
Implementing existing algorithm from STM32 version
NeoGPS, Curie IMU, XBee and Servos Libraries will be used
Admin
Remaining Testing Goals before end of term
end to end sensors (all of which can be tested in ground)
Gemini
Video over LTE
Calibrate Opflow
Monster mount offsets (for rangefinder and opflow)
Four vs Six Batteries test (all require test flights)
Houston Autotune
Pegasus Autotune
Pegasus Four Battery Endurance
Pegasus Six Battery Endurance
Nov 25th
same day as open house
Nov 26th
Remaining possible flight dates for this term:
Dec 2nd
Dec 3rd
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