đź“‹ Admin Preparation
Requested By | |
---|---|
Goal Summary | Final test before competition. |
Status? | DRAFT / SUBMITTED / WAITING FOR SUB-TEAM REVIEW / APPROVED |
Desired Airframe | Pegasus 1 |
Date(s) | 18th May 2024 |
🥅 Testplan
Necessary Preparation
Explain what capacity you need, what needs to be mounted, etc.
Necessary items:
Jetson
CV camera
< rfd900 >
etc
Flight characteristics needed:
Flight speed
flight distance
max altitude
< etc >
Comms / Support needed:
Autonomous/repeatable missions
ability to hold location within +/- X meters
FPV Video from the drone?
etc….
đź«‚ Mandatory Attendees
This is a section for all attendees from your subteam which will be present for this flight test. (because they are testing their products, or otherwise)
Name | Phone # | Sub-team | Role |
---|---|---|---|
 Smile Khatri | 8076320853 | Mech |
|
Flightline Team
Name | Phone # | Role | Reason |
---|---|---|---|
 |  |  | |
Pre-Flight Checklists
⏲️ Flight Test Timeline
note test 1 is competition task 1 and test 2 is competition task 2
Date/Time | Action | Notes |
---|---|---|
lunch time ish | Briefing @ WARG Bay | Â |
Arrival at Flight Test Location | Â | |
Experiment with tracking antenna | Â | |
 | Bring equipment to flightline |  |
Test1 card 1 | Hardy Yu manually track the drone RTL because RC failsafe | |
Configure direct binding phrase to use normal controller elrs instead of gemini | ||
 | Test 1 card 1 | |
Test 2 card 1 practice #1 | ||
 |  Test 2 card 1 practice #2 | |
 |  switch battery |  |
Test 2 card 1 practice #3 | ||
Test 2 card 1 practice #4 | ||
Test 2 card 1 practice #5 | ||
Presentation Photos | ||
Start 4:30pm | Debrief |
đź’» DEBRIEF
Flight test debrief report
Before Card 1:
Before departure
Yuchen Lin didn’t logistic going to flight test → next time book the car beforehand + long weekend machine shop does not open
Yuchen Lin Hardy Yu Testing with huston → connected to mission planner and able to forward the message(test 2 times)
first one does not flash the latest code
second one see tracking antenna working as expected
After departure
pre-flight tracking antenna testing: (no code change)
Keep rotating without stop and does not work
After adjust to the north keep rotating clockwise
does not help after adding delay
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Card 1 Test 1
Flight planning
conduct half task 1 goal (1.5 lap)
Flight test card requirements/objectives Performance
Comp sim
Control performance & payload situation
Four payload in the cabin + alien key
Hardy Yu manually track the drone
Identified issue
Compass variance issue
place the drone backward and cause sharp turning
Issue need to be RCA
 Gemini not working (performance worse than without gemini) → fully lost link
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Card 1 Test 1 retry 1
Flight planning
conduct half task 1 goal (1.5 lap)
Flight test card requirements/objectives Performance
Check tuning in all three mode and compass variable at full throttle.
Control performance & payload situation
Four payload in the cabin
Current draw pretty good at calm weather
half of task 1 5000mah
Identified issue
aggressive takeoff
Almost all the time ekf yellow
Issue need to be RCA
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Card 3 Test 1
Flight planning
Test the auto mission task 2 pathing and training pilot for landing
Flight test card requirements/objectives Performance
During flight time upload the mission to pixhawk
Arm in auto and complete the mission
Pilot navigate through and land on the pad with fpv goggle
Control performance & payload situation
Four payload in the cabin
GSO and pilot get familiar with callout (Better callout procedure for less than 1 meter → with range finder) practice next week
Identified issue
Need to document the process for uploading the mission during flight test
Video quality become bad when antenna not point at drone(comp → manually turn it)
Pilot navigation pattern (desend and find the pad)
Upload the mission will kill the tracking antenna → soln? hardcoded
Disarmed 6 inches above the ground reason hard to land exact
Gps to non-gps transition test!!!
SD card was installed in FPV goggles but automatic recording did not start
Issue need to be RCA
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Card 3 Test 2
Flight planning
More pilot training
Flight test card requirements/objectives Performance
pilot familiar landing in loiter
Control performance & payload situation
Four payload in the cabin → complete mission objective
GSO and pilot get familiar with callout
Identified issue
1 min landing window → need timing callout
Broke the 3d printed leg joint during landing
Descending faster
SD card was installed in FPV goggles but automatic recording did not start
Issue need to be RCA
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Overall performance and Lessons learned
Outcomes
confident in flight characteristics of the drone and electrical robsutness
spline waypoints looked good during flight but looks poor on mission plannre
low confidence in custom rf links and tracking antenna
not using tracking antenna for comp → cc Daniel Puratich to bringup at AEAC
Gemini board was low link quality
try another gemini board and see if it works
Nathan Green apply new mag fit data based on today’s data